Alaska Airlines Flight 1282, a Boeing 737 MAX 9, experienced a serious incident on January 5, 2024, when a door plug separated from the aircraft at about 16,000 feet after departing Portland for Ontario. The event caused rapid decompression and left a large hole in the fuselage. All passengers and crew survived, with eight people sustaining minor injuries.
The National Transportation Safety Board (NTSB) has released its final report on the accident, attributing primary responsibility to Boeing for failing to provide adequate training, guidance, and oversight during manufacturing. The report states: “The National Transportation Safety Board determines that the probable cause of this accident was the in-flight separation of the left mid-exit door (MED) plug due to Boeing Commercial Airplanes’ failure to provide adequate training, guidance, and oversight necessary to ensure that manufacturing personnel could consistently and correctly comply with its parts removal process, which was intended to document and ensure that the securing bolts and hardware that were removed from the left MED plug to facilitate rework during the manufacturing process were reinstalled.”
The NTSB also cited shortcomings by the Federal Aviation Administration (FAA). According to the report: “Contributing to the accident was the Federal Aviation Administration’s ineffective compliance enforcement surveillance and audit planning activities, which failed to adequately identify and ensure that Boeing addressed the repetitive and systemic nonconformance issues associated with its parts removal process.”